Improving the Cushcraft 40-2CD Loading Coils The Cushcraft 40-2CD uses 4 loading coils, which they call LCA (Loading Coil Assembly). I had one that had burned out, and when I fixed it, I found a much better way to construct the assembly for mechanical stength. The LCA consists of a heavy-wall plastic tube, around which is would the tinned or plated copper wire of the loading coil. At each end, the plastic form telescopes into the aluminum element tubing. The coil wire is looped under self-tapping screws and the plastic form is fastened to the aluminum tube with 2 large rivets. The assembly is covered with a heat-shrink tube. My antenna, which was the subject of the QST article, has been through an extraordinarily stressful life and doesn't owe me anything. We've had winds up to 134 mi/h, and ultimately the 120' tower, which was overloaded by my commercial renters, broke a guy anchor rod and the whole thing came down. When I was salvaging the pieces to put the 40-2CD back up, I found that one of the traps had failed to an open circuit where the wire was terminated. The wire had a copper ball from melting in an arc, and my conclusion is that the failure had occurred before the crash. It appears that the wire had fatigued and broken because the rivets had become loose from flexing in the wind, allowing motion of the plastic form in the aluminum element tubing. The cracked wire then arced until the gap was too great to bridge. When I had originally built the antenna, I was aware that the self-tapping screws had a reputation of rusting out from moisture getting into the trap from the inside (although the outside is covered with heat-shrink, the inside is open to the weather through the element joints). I had replaced the self-tapping screw with a 10-32 x 1" pan-head stainless machine screw with internal-tooth lock washer and nut. I've heard that Cushcraft now uses an approach like this in new antennas. Because I've had some failures of stainless hose clamps have seen some rivets eat an oversized hole in element tubing, I now assemble all highly-stressed element joints with two stainless bolts with nylon insert locking nuts (whether I use a hose clamp or not; as an aside, I buy exact bolt lengths, such as 7/8" and 1 1/8", so I don't have anything sticking out of the nut to snag on guys or whatever). When I was reassembling the traps, I drilled out one of the rivets that was roughly at a right angle to the coil-terminating screw and put another 10-32 x 1" screw through the element and plastic form (at both inner and outer ends). This double shear and compression results in a very much stronger mechanical assembly that I believe will not become loose over time. If I were building the loading coil from scratch, on assembly I would also coat the tips of the form with something waterproof and rubbery such as polyurethane caulk (much better than RTV, butyl or silicone, but for some reason not easy to find). I would also consider using the heat-shrink tubing that comes with a meltable sealant on the inside surface. The only mechanical failures I had experienced with the original strengthened antenna were U-bolts eating their way through relatively thin element-to-boom plates and failure of inner ends of the outer boom sections, which were too thin to withstand the torsional load of the heavy reinforced elements. This is no knock on Cushcraft, as the antenna was exposed to winds far above even the 118 mi/h upgrade level I had worked to. For the reborn antenna, I used a single 24' length of extruded 2" diameter 0.12" wall 6061-T6 tubing for the boom, and made new element and boom mounting plates from 3/8" thick 6061-T6 plate. Both the elements and boom are mounted with 2" plated muffler clamps (with the heavy material, you can really tighten up, so there's no tendency for the elements to rotate on the boom). The boom is guyed from above with two cables on each side, after the fashion of the HyGain LP1009 (the guys come from a single point on the mast down to each end of an 18" aluminum angle attached to the boom as if it were a short dummyh element). This seems to prevent failure from rotary motion of the elements and boom, and is working out well on other antennas I have up. After I straightened the elements and put the antenna back up, the 40-2CD works great again, even in comparison to my reference antenna, a near-full-size capacitively loaded rotary dipole in a somewhat more favorable location. We've had our first big winds of the season without any antenna failures, so the mechanical setup seems sound. As a final comment, I got immediate and very helpful response from Cushcraft when I needed replacements for the parts that had been scraped off in the crash. Dave, W6NL